[AR] Re: Successful liquid launch at FAR

  • From: Robert Watzlavick <rocket@xxxxxxxxxxxxxx>
  • To: arocket@xxxxxxxxxxxxx, Paul Breed <paul@xxxxxxxxxx>
  • Date: Tue, 18 Jan 2022 21:49:37 -0600

Paul,

On 1/18/22 3:39 PM, Paul Breed wrote:

Robert,
A couple of questions....

If you were doing it again, what would you change?
Specific questions about the design as flown...

Vehicle-wise:
1.  I would have put the GHe (tank pressurization) and GN2 (pyroless) fill ports lower on the vehicle for easier access.  I also would have made the access panel larger and probably out of a thicker material than the 0.016 inch thick skin.  I already was going to place some aluminum tape over the DZUS fasteners anyway since they were kind of loose but when I broke off the access panel hinge rivets on the pad, I ended up taping over the entire panel. The access panel for the avionics bay worked much better since it was made out of the 0.1 inch thick fiberglass reinforced phenolic body tube.  I think keeping the avionics switch panel fwd on the vehicle and away from the hot flamey stuff is still a good idea since a burn through of those wires would prevent moving the valves to a safe position in the event of a fire.  A larger pressurization access panel would have also helped because at 3000 psi, the pin depressor in the strut valve was really hard to turn by hand.

2.  I should have found a better place to put the telemetry antennas.  They were in the recovery bay right next to the GPS antenna which required a special GPS antenna with a filter to reject the 900 MHz primary TM signal.  The GPS antenna was supposed to be in the avionics bay (that's why it was fiberglass/phenolic) but the EMI from the flight computer swamped the uBlox GPS receiver.

3.  I would have made the vehicle with a smaller aspect ratio.  The long skinny design has stability issues with wind, which fortunately weren't a problem on Saturday.  The design though was driven from choice of modified oxygen cylinders so it didn't make sense to use a larger diameter body.  I liked the oxygen cylinders though since they had a thick heel to put a boss port into and had a neck to use for an inlet fitting.

4.  As you probably noticed, I had a lot of fasteners.  In several places there wasn't enough clearance to use a the floating nutplates so I cut off one ear and used JB Weld to make a Click-Bond style nutplate.  The JB Weld cracked loose in many occasions during build so I should have used MS212061 one-lug nutplates with two fastener holes on one side.  I really liked the floating nutplates though because they compensate for misaligned holes between the skin and stringers.  And they allow you to take the skins on/off on the accessible bays without worrying about stripping out threaded holes in the stringers.  A lot of people commented "wow, that's a lot of screws!"  Yes, that's true but my informal survey  shows skin/stringer construction to be the lightest option at 0.36 lbm/ft. The closest was PML CF ultralight with a 0.040 wall and that came in at 0.44 lbm/ft.  I think the PSAS team had a honeycomb sandwich design that was super light though.  The main thing you gain with a skin/stringer design is good access for tubes, wrenches, etc.and lots of places to attach things to the flanges.

5.  I should have made the flight computer smaller and/or more easily removable.  It consists of three boards, a power supply, a microcontroller board, and an analog signal conditioner board. Luckily I didn't have any failures but it would have been a real pain to get any of those boards out for replacement, especially since there's a shared heatsink for the TM transmitter and power supply board that ties into the airframe.

6.  I used miniature Endevco/Kulite analog sensors with millivolt output but it would have been nice to have all digital sensors as I could have eliminated the signal conditioner board.  However, using all digital sensors implies potentially using a common bus which could be a single point failure.

7.  I was worried about FOD or dripping water from the LOX tank getting into the main valve servo.  I made a makeshift rain cover out of some aluminum tape but it would have been better to completely encapsulate the gear assy and servo in some kind of 3D printed cover.  There's not much room down there though.

8.  I should have used 0.028 wall aluminum tubing instead of 0.035 tubing to save weight and make it easier to bend.

9.  If I had tried harder, I could probably have shortened the vehicle by 1-2 feet by making some custom manifolds instead of the ratsnest of tubing in the pressurization and engine bays.

10.  I considered adding externally powered solenoid valves to depressurize the tanks in the event of a flight computer failure but they were big and heavy.  Luckily I didn't have a problem.  My argument against it was that the helium tank was DOT rated and the LOX tank had a burst disc which would have self-relieved.  The fuel tank could have remained pressurized though.  If there had been an explosion on the pad, backup valves might not have helped anyway so the Winchester depressurization method might have had to be used (not sure if FAR has a rifle on hand - haha).

11.  A slightly longer recovery bay (by a few inches) would have made it easier to pack the parachutes.

12.  Stronger magnets on the umbilical or perhaps a different design would have avoided that last minute trip to the pad.  There was only minimal clearance between the ground side of the umbilical disconnect and the launch rail so when I was disconnecting the LOX fill hose, I likely bumped the rocket enough for the umbilical to pop off.  I wanted to avoid the fins getting snagged on the umbilical so I had to add a bungee to pull them away at launch but that reduced the hold force that the magnets provided.  The umbilical could have been placed near the base of the vehicle but then you have a lot of wires running through the engine bay which isn't ideal.  There are other disconnect ideas out there I've seen but I just though the magnetic was kind of different so I thought I'd try it.

13.  Software-wise, I wish I had completed the moving map (I ran out of time) so I would have had better situational awareness of where the rocket was during descent.

14.  The threaded end cap for the the spring loaded SAFE/ARM switch rattled off during the trip out there.  I used blue threadlocker on all non-locking fasteners but I missed that one.  Luckily I noticed it prior to launch.

Things that didn't work:
14.  I tried to use a spring scale to measure the weight of the vehicle to ensure I completely filled the LOX tank.  During a static test one time, I thought I had plenty of LOX loaded but apparently it was only half full.  The vehicle/rail combination had too much friction so I didn't end up using the spring scale.  I wish there were some reasonable solutions for cryogenic level sensing.

15.  I added a small needle valve to vent the LOX hose prior to disconnect but it froze up and I couldn't turn it.  I ended up disconnecting the LOX fill hose under pressure which provided a little excitement.  I had purchased a Rego valve like they use on the dewar but it was really heavy and I was worried it would put too much moment on the LOX fill port without some sort of support.


Were all valves driven by AX12A servos?
Yes - there were 4 servos, one for the GHe supply, directly connected to a Swagelok SS-4P4T valve: http://www.watzlavick.com/robert/rocket/rocket1/photos/dsc_1174m.jpg
The Fuel and LOX vent valves were directly connected to my modified Swagelok SS-62T6 ball valves: http://www.watzlavick.com/robert/rocket/rocket1/photos/dsc_1191m.jpg
The main valves were ganged together with a 3:1 gear reduction: http://www.watzlavick.com/robert/rocket/rocket1/photos/dsc_0081m.jpg, http://www.watzlavick.com/robert/rocket/rocket1/photos/dsc_0080m.jpg
I liked the smart servos vs. traditional RC servos because you can read back the position, torque (really just the current), temperature, etc. And if you lose power, they stay in the last position.
What exactly did you use for the He pressure regulators?
Aqua Environment 1247-1, with the female NPT inlet modified to be a -6 boss port.  I really hate NPT fittings so I wanted to get rid of as many as possible.  There are Aqua 955 check valves on the outlets.

What did you use for ignitor valves?
GEMS A2012-2M-OC-V-VO-C204 solenoid valves, same as I had on the test stand.  They are fairly heavy (~0.5 lb) and they were 24 VDC so I had to power them externally via the umbilical. I could have got them in 12 VDC to power from the vehicle but the current plus the AX-12A servos would have required a voltage regulator more than the 2 A one I had selected.  Plus, I wanted to minimize the electrical noise from the solenoids - they're controlled by an opto-isolated SSR.

Did you do anything special to keep your ball valves tight?
A lot of times people put Belville washers on 3 pc Lox valves to keep the valve tight as temps change?
Any seal/thermal issues with what appears to be stainless Steel ball and aluminum body? (I could have that wrong)
Any more details on the seals in the lox ball valve?
I kept the ball, PTFE seals, and Belleville washers from the Swagelok SS-62T6 valves.  I never had a problem with downstream leakage past the ball.  The main problem was with the stem seals and we had a discussion on that a while back on aRocket.  I wanted to reduce the actuator torque when cold so I used spring energized PTFE seals.  They sort of worked with a small amount of leakage which I fixed by using two seals and pressurizing the cavity between them with the helium supply.  They still leak a bit during tank pressurization but once LOX starts flowing, there should be a slightly higher pressure at the gas supply vs. at the valve because of the pressure drop through the plumbing.  Once I did that, the leakage out the valve was very small.  The fuel valves are leak free of course.  I used #10-32 aluminum bolts to hold the valves together instead of SS to save a lot of weight and to self-compensate for thermal differences.  It would be nice if some university group could take the existing design and improve on it to make it leak free (hint hint) but still being cheap to make and controllable by a small servo actuator.

You put purge bags around the valves/actuators..
If you were going to do it again would it be earlier to just make the rocket body panels purge tight?
I put the purge bag around the valve because I have open bearings (so I can clean them for LOX) and during multiple back-to-back LN2 tests, water condensed in the bearings and froze.  It would be really hard I think to make a skin/stringer design air tight.  Well, maybe not with appropriate seals - airplane access panels are usually well sealed against moisture.  But between bays, there were big holes in the body frames with wires and tubes running through them which would be hard to seal.

Do you have a total weight breakdown for all the components?
SEe http://www.watzlavick.com/robert/rocket/rocket1/design/rocket1_mass_properties_public_20220120a.xls
The as-flown configuration had about 16 sec of fuel and apparently 10 sec of LOX so the final weight was slightly less than the spreadsheet.

Again congratulations on a fantastic flight!
Thanks!  And thanks for coming out to see it and helping to recover it.

-Bob

Paul



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